1” Radial Cutting Torch Cut Stuck Coiled Tubing Under Compression After One Year of Operation Suspension

Overview Challenges2” Coiled Tubing Stuck at 3,800mDeviation 10.95 Deg ̊5 ppg Brine3668psi @ 1720mTemperature 205 ̊ FMin Restriction 1.06 inchContinuos pressure surface pressure built upStringent Lithuim battery importation regulationsCT suspected…

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Rapid Deployment of Memory PTC Puncher on Coiled Tubing Reinstate Back Gas Well Production as Main Supply for Gas Injector Well

Overview Challenges Highly deviated well (77 degree) Coil tubing memory conveyance Required minimum flow area of 3.8-sqinch Solutions Non-explosive puncher on memory conveyance Details One of major oil and gas…

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Rapid Mobilisation of Non-Explosive Puncher Enable Customer to Complete Cement Squeeze Operation at Remote Offshore Location

Overview ChallengesRestriction of 3.313” IDSlickline / memory conveyanceChallenging to mobilise explosive in countryUnknown well historySolutionsNon-explosive puncher on memory coveyance Details Over 40 fruitful years of oil production, the wells have…

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Successful 2″ Coil Tubing Recovery in Natuna Sea

Overview Challenges•  2" Coil Tubing stuck due to runaway after cement job•  Top of cement 9,950ftMD•  45.56 Deg deviation•  No circulation•  8.3ppg fluid•  Restricted rig up heightsSolutions•  PTC/RCT deployed utilizing…

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